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Corporate Information

 
Press Release (Dec 01,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 10:00 am, December 1)
 
*Updates are underlined. 
 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
 
Unit 1 (Shut down) 
-Explosive sound and white smoke were confirmed after the big quake 
 occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line.
 The current water injection volume is approx 4.2m3/h from the reactor 
 feed water system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at 
 1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. 
-On October 28, we completed installation of the cover for the Reactor 
 Building in order to contain dispersion of radioactive substances.
-At 4:04 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. At 4:08 pm on November 30, injection amount 
 reached the scheduled amount of 5 N m3/h. 
 
Unit 2 (Shut down) 
-At approximately 6:00 am on March 15, an abnormal noise began emanating 
 from nearby Pressure Suppression Chamber and the pressure within the 
 chamber decreased. 
-At 10:10 am on March 26, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line. 
-At 2:59 pm on September 14, we started injecting water to the reactor 
 through core spray system water injection piping arrangement in addition 
 to the water injection through reactor feed water system piping 
 arrangement.
 Water is currently injected at approx. 3.1m3/h through reactor feed water 
 system piping arrangement, and at approx. 4.3 m3/h through core spray 
 system water injection piping arrangement.
-At 5:21 pm on May 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. (We started injection of hydrazine from 
 1:26 pm to 3:04 pm on November 30).
 At 11:13 on November 30, the alarm went off at the alternative cooling 
 system in the Fuel Pool Cooling and Filtering System indicating that the 
 difference of the flow rate between at the inlet and at the outlet is 
 large and the system automatically stopped its operation. At 11:34 pm on 
 the same day, no leakage was confirmed by the site inspection. At 11:00 
 pm on the same day, the temperature of spent fuel pool was 22.7 °C and 
 the anticipated temperature increase was 0.3 °C/h. As there is sufficient 
 buffer, the inspection is scheduled during the morning of December 1. 
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary 
 Containment Vessel.
-From 6:00 pm on October 28, we put the gas management system of the 
 reactor containment vessel in operation.
-At 11:04 am on November 6, we started operation of radioactive material 
 decontamination instrument of spent fuel pool.
-At 1:45 pm on November 30, we started nitrogen injection to the Reactor 
 Pressure Vessel. At 2:47 on the same day, as we confirmed nitrogen 
 injection had not increased, we temporally stopped the operation. The 
 cause is under investigation. We are continuing nitrogen injection into 
 the primary containment vessel. 
 
Unit 3 (Shut down) 
-Explosive sound and white smoke were confirmed at approximately 11:01 am 
 on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray 
 system in addition to water injection by the reactor feed water system 
 piping arrangement. 
 Water is currently injected at approx. 2.1 m3/h through reactor feed 
 water system piping arrangement, and at approx. 6.1 m3/h through core 
 spray system water injection piping arrangement.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary 
 Containment Vessel started. 
-At 4:26 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. At 4:40 pm on November 30, injection amount 
 reached the scheduled amount of 5 N m3/h. 
 
Unit 4 (Outage due to regular inspection) 
-At around 6 am on March 15, we confirmed the explosive sound and the 
 sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-Regarding spent fuel pool for unit 4, from August 20 to November 8, we 
 had decreased salinity by using the desalting facility. In order to 
 decrease more salinity, we installed Ion exchange equipment and started 
 the equipment at 10:58 am on November 29.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
 
Unit 5 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump 
 in order to cool the spent fuel pool.
-At 2:30 pm on March 20, the reactor achieved cold shutdown.
-At 2:45 pm on July 15, we started the operation of the original Residual 
 Heat Removal System (System B) by its original seawater pump.
-From November 28, we started cleaning to avoid the performance 
 deterioration of pumps by sucking up sands etc. accumulated at the bottom 
 of the inlet canal pump room.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
 
Unit 6 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
 of Unit 6 to cool down Spent Fuel Pool.
-At 7:27 pm on March 20, the reactor achieved cold shutdown. 
-At 2:33 pm on September 15, we started separately cooling the reactor 
 through the Residual Heat Removal System and the spent fuel pool through 
 Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage 
 inside PCV. 
 
Others 
-At around 10 am on June 13, we started the operation of the circulating 
 seawater purification facility installed at the screen area of Unit 2 and 
 3.
-At 8 pm on June 17, we started operation of Water Treatment Facility 
 against the accumulated water. At 6:00 pm on July 2, we started the 
 circulating injection cooling to inject the water, which was treated by 
 the accumulated water treatment system, to the reactors through the 
 buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by 
 parallel operation of one line from the cesium adsorption instrument to 
 the decontamination instrument and the other treatment line of the cesium 
 adsorption instrument No.2. 
-At 2:06 pm on October 7, we started to spray purified accumulated water 
 brought from Unit 5 and 6 continually in order to prevent dust scattering 
 and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea 
 side, in front of the existing shore protection, Units 1-4, in order to 
 contain marine pollution by underground water.
-At 9:25 am on November 15, we started transfer of accumulated water from 
 basement of Unit 3 turbine building to Centralized Radiation Waste 
 Treatment Facility Building.
-At 6:03 pm on November 30, we started transfer of the accumulated water 
 from the basement of Unit 2 turbine building to Centralized Radiation 
 Waste Treatment Facility High Temperature Incinerator Building. 
-At 10:00 am on December 1, we started transfer of the accumulated water 
 from Unit 6 turbine building to Temporary Tank. 
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